dynoed today !!!!!! 272 WHP 223 WTQ stock block LS
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dynoed today !!!!!! 272 WHP 223 WTQ stock block LS
Whats up everyone, i Dyno'd today at DSR !! and my what a day it was !! heres my set up
93 civic DX coupe
95 integra LS motor
Skunk 2 cam gears
Action 2MD clutch
lovefab equal length manifold ( GOOD STUFF CODY !)
internal gated T3 super 60 turbo ( garrett purcahsed from cheapturbo.com)
2.25 1st bend dp flared to 2.5 with Mccord cut out( i love this thing!!) DIY
Turbo XS RFL
DIY 2.5 inch mandrel bend charge from outlet of IC and 2 inch from turbo to IC
custom 31X6X3 intercooler bar n plate core
CPR 440CC injectors from viren
hondata S200B from KS-motorsport ( who sent me the wrong base map and lost me 30 min off my dyno time because Dynospotracing had to create me the actual base map i asked for 440CC W/ 3 bar map and 8K RPM redline instead of stock honda map and 8500 redline)
GM 3 bar map sensor
1st dynotune i got 206.2 and 179 torque, to my suprise lawrence later informed me that the hondata was not even working * because i put J1 on a switch, the car would only work witht eh switch position off so i figured it may have been somethgin with the switch. he took the chip out and looked at what was on it and told me it was set for a honda map and not a 3 bar as well as an 8500 RPM redline hence why my car wasnt working with the hondata ON. He said my car must've been running with just 440's and the GM 3bar and way the hell retarded ignition *( DAMN IM GLAD I DID THAT !!!) let me tell you guys, he said the top end on my 200 WHP run @ 10 psi was cherry smooth as a babys bottom. however 2.5-4.5 K was very lean, hence my hesitation problem. If someone can figure out how to mimic the lower range of the RPM band it could be a pretty nice fuel set up for the DIY enthusiast.
anyways lawrence reburned my chip and i instantly dropped to 175, this made my heart sink but he said the timing was way retarded on the distributor as well as the hondata, so we proceeded to put the car back to stock timing and wala !! 224 WHP. We tuned for 14 psi and ran my amazin 272.4 ( at this time im jumping for joy and shitting my pants because i was thinkin i'd only be gettin 250 or so at most). He tuned my cam gears and it made my wastegate spike a little hitting boost cut which is at 15 psi. SO we lowered the boost by 1 psi and it still put out about 265 HP. Non the less im totally stoked and lookin for more traction. Thank you honda-tech !! for making me a beliver in fine tuning and stock blocks !!!!!!!!
dyno will be up shortly once i get it scanned. thanks for reading everyone.
93 civic DX coupe
95 integra LS motor
Skunk 2 cam gears
Action 2MD clutch
lovefab equal length manifold ( GOOD STUFF CODY !)
internal gated T3 super 60 turbo ( garrett purcahsed from cheapturbo.com)
2.25 1st bend dp flared to 2.5 with Mccord cut out( i love this thing!!) DIY
Turbo XS RFL
DIY 2.5 inch mandrel bend charge from outlet of IC and 2 inch from turbo to IC
custom 31X6X3 intercooler bar n plate core
CPR 440CC injectors from viren
hondata S200B from KS-motorsport ( who sent me the wrong base map and lost me 30 min off my dyno time because Dynospotracing had to create me the actual base map i asked for 440CC W/ 3 bar map and 8K RPM redline instead of stock honda map and 8500 redline)
GM 3 bar map sensor
1st dynotune i got 206.2 and 179 torque, to my suprise lawrence later informed me that the hondata was not even working * because i put J1 on a switch, the car would only work witht eh switch position off so i figured it may have been somethgin with the switch. he took the chip out and looked at what was on it and told me it was set for a honda map and not a 3 bar as well as an 8500 RPM redline hence why my car wasnt working with the hondata ON. He said my car must've been running with just 440's and the GM 3bar and way the hell retarded ignition *( DAMN IM GLAD I DID THAT !!!) let me tell you guys, he said the top end on my 200 WHP run @ 10 psi was cherry smooth as a babys bottom. however 2.5-4.5 K was very lean, hence my hesitation problem. If someone can figure out how to mimic the lower range of the RPM band it could be a pretty nice fuel set up for the DIY enthusiast.
anyways lawrence reburned my chip and i instantly dropped to 175, this made my heart sink but he said the timing was way retarded on the distributor as well as the hondata, so we proceeded to put the car back to stock timing and wala !! 224 WHP. We tuned for 14 psi and ran my amazin 272.4 ( at this time im jumping for joy and shitting my pants because i was thinkin i'd only be gettin 250 or so at most). He tuned my cam gears and it made my wastegate spike a little hitting boost cut which is at 15 psi. SO we lowered the boost by 1 psi and it still put out about 265 HP. Non the less im totally stoked and lookin for more traction. Thank you honda-tech !! for making me a beliver in fine tuning and stock blocks !!!!!!!!
dyno will be up shortly once i get it scanned. thanks for reading everyone.
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Re: dynoed today !!!!!! 272 WHP 223 WTQ stock block LS (SDT Project EF)
hey CJ post up some pics of my coche . gracias.
here are some pics i took outside of the shop earlier yesterday
Modified by project dc2 at 11:51 PM 8/29/2003
Modified by project dc2 at 12:04 AM 8/30/2003
here are some pics i took outside of the shop earlier yesterday
Modified by project dc2 at 11:51 PM 8/29/2003
Modified by project dc2 at 12:04 AM 8/30/2003
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Re: dynoed today !!!!!! 272 WHP 223 WTQ stock block LS (u2civic1)
<TABLE WIDTH="90%" CELLSPACING=0 CELLPADDING=0 ALIGN=CENTER><TR><TD>Quote, originally posted by u2civic1 »</TD></TR><TR><TD CLASS="quote">isn't 14psi alot for a stock block even tho its tuned</TD></TR></TABLE>
no..
no..
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Re: dynoed today !!!!!! 272 WHP 223 WTQ stock block LS (u2civic1)
<TABLE WIDTH="90%" CELLSPACING=0 CELLPADDING=0 ALIGN=CENTER><TR><TD>Quote, originally posted by u2civic1 »</TD></TR><TR><TD CLASS="quote">isn't 14psi alot for a stock block even tho its tuned</TD></TR></TABLE>
Depends on the turbo, 14psi on a precsion sc63 or something huge would be alot for a stock block.
Depends on the turbo, 14psi on a precsion sc63 or something huge would be alot for a stock block.
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Re: dynoed today !!!!!! 272 WHP 223 WTQ stock block LS (01SILVERDC2)
<TABLE WIDTH="90%" CELLSPACING=0 CELLPADDING=0 ALIGN=CENTER><TR><TD>Quote, originally posted by 01SILVERDC2 »</TD></TR><TR><TD CLASS="quote">nice, well lets see the dyno sheets </TD></TR></TABLE>
yeah i wanna see that dyno chart. So how much was that manifold?
yeah i wanna see that dyno chart. So how much was that manifold?
#16
Re: dynoed today !!!!!! 272 WHP 223 WTQ stock block LS (project dc2)
stupid phil and his stupid civic running a stupid 272 whp and 223 wtq when my sexy wrx is running an unsexy 250 hp cause its too close to stupid stock....STUPID PHILL!!!! hahaha j/k good **** phil...that suprised us both. u jerkface im proud to say and me dean helped work on this stupid car.... even though we did really basic stuff. next project....turbo dean????
chris
chris
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Re: dynoed today !!!!!! 272 WHP 223 WTQ stock block LS (itsall****)
nice!! almost the same amount of power i'm putting out. although your power curve looks like a somewhat like a vtec motor's curve. check out my curve...same psi as you're running but with 8.8:1 pistons and t3/t4e .63 a/r .60 compressor .57 trim. although i wish my torque curve were something like yours.
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Re: dynoed today !!!!!! 272 WHP 223 WTQ stock block LS (SDT Project EF)
You should have rev'd it higher. The torque hasn't even started to drop off. There must have been more power up top
<TABLE WIDTH="90%" CELLSPACING=0 CELLPADDING=0 ALIGN=CENTER><TR><TD>Quote, originally posted by SDT Project EF »</TD></TR><TR><TD CLASS="quote"> </TD></TR></TABLE>
<TABLE WIDTH="90%" CELLSPACING=0 CELLPADDING=0 ALIGN=CENTER><TR><TD>Quote, originally posted by SDT Project EF »</TD></TR><TR><TD CLASS="quote"> </TD></TR></TABLE>
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haha dammn phil...called me and he was all excited...something bout trying to peer pressure me into making my car fast hahahah u suck
good job man
good job man