Cracked my Rad today ARRGH..
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Cracked my Rad today ARRGH..
well, I went to the track today, about an hr drive both ways.. When we got there, it started raining so we just came back home..
THing is, when i got to my driveway, i noticed that my stock teg radiator developed a hairline crack on the front/top of the plastic endpiece of the radiator.. i dont know how long i was driving w/ it cracked, but there was a noticable amt of coolant leakage by the coolant visable throughout the engine bay and on the hood.. I"m guessin it cracked on my way home, but i cant verify WHEN it cracked..
I never noticed my temp gauge temp goin up, so i never suspected any thing wrong in the engine bay.. Keep in mind that I"ve got 2 fans on the rad, on in front and one in the stock location.. I"m jsut curious why it even cracked, considering today wasn't even a warm day...
Any help would be appreciated..
THing is, when i got to my driveway, i noticed that my stock teg radiator developed a hairline crack on the front/top of the plastic endpiece of the radiator.. i dont know how long i was driving w/ it cracked, but there was a noticable amt of coolant leakage by the coolant visable throughout the engine bay and on the hood.. I"m guessin it cracked on my way home, but i cant verify WHEN it cracked..
I never noticed my temp gauge temp goin up, so i never suspected any thing wrong in the engine bay.. Keep in mind that I"ve got 2 fans on the rad, on in front and one in the stock location.. I"m jsut curious why it even cracked, considering today wasn't even a warm day...
Any help would be appreciated..
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Re: Cracked my Rad today ARRGH.. (BigBooster)
<TABLE WIDTH="90%" CELLSPACING=0 CELLPADDING=0 ALIGN=CENTER><TR><TD>Quote, originally posted by BigBooster »</TD></TR><TR><TD CLASS="quote">good excuse to get a fluidyne.</TD></TR></TABLE>
They suck, mine ballooned when I cracked my sleeve on my GSR block running 10 psi.
They suck, mine ballooned when I cracked my sleeve on my GSR block running 10 psi.
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Re: (Boostfed)
well.. $$ is tight now so i'm just gonna throw a civic AUTO radiator in there for the time being.. if it happens again, i'm definately upgrading to a PWR half size rad..
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Re: (92HB_HB)
Alright, i got the civic rad on now , and today i noticed that my upper rad hose began to bulge around the 90 bend.. This is the exact same hose that i used on the teg radiator too..
never seen this happen b4 either.. I think i'm gonna get some steal tubing and use that instead of them dam OEM rubber rad hoses..
never seen this happen b4 either.. I think i'm gonna get some steal tubing and use that instead of them dam OEM rubber rad hoses..
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Re: (m R g S r)
I surely HOPE its not blown.. I dont have any CLEAR symptoms of a blown HG.. i.e.
-milky coolant
-coolant over flowing into overflow tank
-high temp gauge readings
-coolant over flowing when reving w/ the rad cap off
-no white smoke out the tail pipe..
-compression was 195-190-190-190, +/- 3psi when i did the test about a week ago..
My built motor has about 8K miles on it now and i've taken it on a few 12 hr trips already.. car pulls pretty good w/o any noticable smoking out the tail pipe either..
runnin a COMETIC .36 mls HG, ARP studs, and was torqued to 70 ftlbs in the proper sequence..
I'm kinda gettin worried though..
-milky coolant
-coolant over flowing into overflow tank
-high temp gauge readings
-coolant over flowing when reving w/ the rad cap off
-no white smoke out the tail pipe..
-compression was 195-190-190-190, +/- 3psi when i did the test about a week ago..
My built motor has about 8K miles on it now and i've taken it on a few 12 hr trips already.. car pulls pretty good w/o any noticable smoking out the tail pipe either..
runnin a COMETIC .36 mls HG, ARP studs, and was torqued to 70 ftlbs in the proper sequence..
I'm kinda gettin worried though..
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